Monthly Archives: March 2011

Finishing touches

On Monday I managed to get over to Martin at Studio 1 Grafix who I’d been in touch with about vinyl. He had a roll of green vinyl that looked a pretty close match so I got a nice length of that along with some advice on applying it. I then nagged David to produce the logos to get them cut out of vinyl and emailed them over to Martin. Monday evening saw the catch tank completed, then I altered the gearshift cable moving the attachment point at the paddle end in towards the pivot, meaning I had a greater throw at the paddle end but more leverage. There had also been a couple of locknuts missing off the rear suspension pullrods and I’d ordered some more from McGill Motorsports who supply loads of rod ends and half nuts etc. Fitting these actually turned out to be a bit of a PITA as with the spring fitted it was difficult getting the pullrod bolts back in.

I then made a start on the steering wheel button wiring. The DigiDash Pro comes with 4 little buttons to go on the wheel that control the functions of the dash and datalogger, for example setting the GPS lap split points etc. I’d got a length of curly cable to allow the wheel to be removed and once I had drilled the holes in the wheel I set about soldering the wires onto them. This was OK except I’d been a bit ham-fisted with the soldering iron and had got the terminals on one of them a bit too hot and the button was no longer working. I was all set to go to Maplin for a replacement during the day but in the end got one for the princely sum of 50p from the electronics stall in the market a couple of hundred yards from the surgery.

I fitted the camera next. The Neuros has served me fairly well but it’s not without its problems. The main ones are the requirement to power it up using the little infra-red remote, the lack of ability to see what it’s doing but most of all the fact that if it gets powered off while recording (for instance when you exit the car in a hurry and shut off the kill switch or simply forget and switch off) then you lose the recording. This was most frustrating. So I’ve invested in a new system from DogCamSport. With the bullet cam fitted to the roll bar it was easy enough installing the main box. The great advantage of this is that it runs on a rechargeable lithium battery so no power off problems. It comes with a cigar lighter power lead but i attacked that so it’s wired direct from the fuse box. It also has a nice simple 2 button remote that was easy to mount in the cockpit.

When making the seat I’d been a bit enthusiastic and rushed prior to the last test at Llandow and made a larger mix of the PU foam on one occasion. A larger mix reacts more quickly and I’d ended up dripping some of it on the bodywork. It had sanded off OK with wet and dry but had stained the paint and I’d had to take it back down more or less to primer. So I masked the car up and touched that up with the small spray gun. While that was going off I nipped down to collect the vinyl graphics from Martin at Studio1. He’d done an excellent job of these and gave me a very good deal. I also called in the builder’s merchant and bought a roll of lead flashing to use as ballast.

In the evening I revisited the ride height & corner weights. The rear had changed when I had to put the locknuts on the pullrods and the front had settled a bit and needed raising. Once I had it set at just over 80mm with my bags of sand in there I stuck her back on the corner weight scales. The car was now coming in at 471.5kg, but that was with 19 litres of fuel in the tank. With me and my helmet, HANS etc. in there it was 562.5, just 2.5kg over the minimum weight limit. Trouble is I don’t want to have to finish very race with 16 litres of fuel in the tank! So I reached for the roll of lead flashing. I decided to cut this into pieces that would fit on the floor at the front of the car – there’s a nice little space under the steering rack between 2 chassis rails that tapers as the rails come back meaning that with the lead cut out carefully it was a snug fit in there and couldn’t move anywhere. The 3 metre roll gave me 12 little sheets cut to shape with just a centimetre waste and this stack of 12 sheets just fitted neatly in the space I had intended for it coming to a couple of mm below the top of the chassis rails. I was pretty pleased with this and one I’d drilled through the stack of lead I used a piece of steel bar and a pair of roofing bolts to hold it down.

The car was now tipping the scales at 573kg meaning that I now need just 6 litres of fuel in the tank to make the weight limit which is just about perfect. Without me doing anything the corner weighting was pretty good too the scales showing the diagonal at 49.4%. A minor tweak of one pullrod saw it nearer to 50% and I then locked off all the locknuts. I think it’s quite amazing that the car needs 10kg of lead ballast even with my 90kg in it, with someone like Derek in it it would need loads more.

It was nearly time to finish for the day – the early morning starts and late night finishes were starting to take their toll – and I decided to indulge myself by fitting one of my nice bright green graphics and a race number. I went over the top surface of the bonnet/front cover with the polish first then after a load of measuring and masking tape I got the first BDN logo stuck on followed by my race number. And here’s the result. Rather spiffing I thought :)

I had a helpful chat with Brian after coming in on Tuesday, among other things we discussed towing eyes. Ian had come up with a couple of suggestions for these but I had decided using some 3mm steel cable was probably going to be the easiest to manage without having to cut bodywork away. After our chat I had a fairly clear idea of how I wanted to achieve it and on Wednesday morning I got the front towing loop fitted without any great drama – a 3mm steel bracket bolted onto the front sub-chassis with the cable running from this along the top of the splitter and exiting between the splitter and the bodywork without having to touch the GRP at all. Very pleased. the rear was a bit more tricky but I made a similar bracket to the front but at the top mount of the sub-chassis so the cable would run back through a hole in the aluminium U channel at the rear. I got it all set up but had only bought 2m of cable and didn’t quite have enough.

I then indulged myself a bit more and fitted the BDN S3 graphic to the nearside sidepod. I got a bit more cable from B&Q on the way home from work and soon had the rear towing loop done. Then I got the race numbers and the rest of the graphics on which was very satisfying and really transformed the car.

 

I then called on David for his opinion on what else I should add. His view all along has been that I should leave the car white and after walking round the car with him for a few minutes and both of us thinking out loud about where we could put some more green vinyl I did start to come round to the idea of leaving it pretty much as it is. The green graphics really do set it off transforming it from the base white and I’m really not sure it needs much more.

Thursday morning felt far less pressurised with only a couple of little jobs to do. I cut some wire mesh and got that fitted to the sidepod ducts to prevent rocks and bits of rubber etc. from either dinging the oil cooler on the nearside or getting into the engine bay on the offside. I held these in place with my tried and trusted method of poking cable ties through from the inside then pulling on them and sticking them to the bodywork with masking tape to hold the mesh in place. I then bonded them in place with some PU sealant. The last job of the day was to fit a little LED to act as an indication when the battery master switch is on, I also tidied up a bit of the wiring with some cable ties.

And that’s it, the car’s ready. Llandow Friday, Bromsgrove for mapping Saturday then up to Mallory for the first race on Sunday.

Bits and Bobs

The Sunday after Llandow was mostly a pretty lazy day. The garage was an absolute tip after a few days frantic activity with no time to tidy up, so I cleared up in there before unloading all the tools and stuff from the car. The corner weight scales were still out so I decided to weigh the car, when I’d done it on Saturday morning I’d just been looking at the relative weights. It had been a bit of a palaver too since the ‘normal’ jack won’t fit under the car and the quick lift one pulls it along a bit rather than lifting vertically. So I made a set of ramps I could push the car onto and then roll it straight onto the scale pads. Once that was done I checked the weight. 453.5 kilos with an empty fuel tank, 542.5 with me in the car. I’ll need to add in the weight of helmet, overalls and boots but subtract the eventual seat weight difference (the one currently in there is 6kg) so they should roughly balance out. The RGB weight limit for a rear engined car is 560 kilos, so I’ll need to add 15kg, maybe a bit more. I can use surplus fuel for some of it but not all and using some lead will help even out the corner weights.

Once that was done I fitted the cowl. This was a nice straightforward little job :) I also cleaned up the bodywork where I’d spilled a bit of the polyurethane seat foam on Friday night in my haste. A bit of wet and dry and it soon looked a lot better but it needs a bit more work.

I then wired in the lambda sensor and connected the logging output wires to the DigiDash and connected the laptop up to check it was working OK which it was. I also sorted out a toggle switch to switch the data logging on and off. While monitoring all the sensors on the laptop I also spotted that the fuel pressure was way too high – Brian had noticed this on the little gauge attached to the regulator. The DigiDash said it was 80psi, almost double the specified 44psi. Turning that down had the effect of making the engine idle much more smoothly, unsurprisingly! This was an issue we’d been puzzled about at Llandow. It probably also accounts for the fouled plugs. We also decided that turning the airbox round had made it impinge a bit on the secondary butterfly valve motor so I popped that off and ground a bit of plastic off to make it sit better without causing problems.

On Saturday I’d run with the Power Commander disconnected. I’d sorted a map ready on the laptop but had then forgotten the laptop in my rather frazzled state. It didn’t really matter as it ran fine and I know Tony Gaunt has run his 06 ZX10 engine for 2 seasons without one. I do want to get it mapped though partly for safety’s sake but mainly to maximise driveability and get rid of the slight flat spot. So on Monday I connected the Power Commander up and uploaded my map to it. This was easy enough but as soon as I connected the PC inline with the fuel injection loom the engine wouldn’t start. I tried resetting it which made no difference then tried a firmware update but that failed.

Although the DigiDash has GPS it still needs the sensor with its magnets connected – it’s an IVA requirement but I think the DigiDash needs it to calculate the gear indication. The plan was to somehow mount this on one of the front uprights with the magnets glued onto the hub. Looking at it this would be easy enough mounting the magnets on the disk carrier but I was a bit worried what effect the heat might have on the araldite so I opted instead to mount them on the machined inside face of the stub axle itself. I made up some aluminium bracketry then removed the stub axle. Past experience tells me simply gluing magnets to the prop on the Fury led to said magnets disappearing, having said that that might have been partly due to the prop vibrating due to the yoke not fitting onto the gearbox output flange properly. So I drilled a couple of shallow holes for the magnets to sit in then glued them in place. Once it was all fitted I got David to spin the wheel and checked it was working.

I’d been hoping to get the Power Commander mapped prior to racing the car but of course couldn’t book anything until I could be confident it would be ready. So when I rang PDQ and they couldn’t fit me in I wasn’t exactly surprised. Austen has booked into HLM in Bromsgrove so I gave them a ring and Hamish there was very helpful and although he couldn’t fit me in this weekend he suggested I call there on the way up to Mallory a week Saturday. He also suggested the recalcitrant Power Commander might be a simple earth issue, he reckons they need a really good earth otherwise they play up. Interestingly he reckons they’re bomb-proof and was sceptical of reports of failures. I didn’t recite the list we’ve got in RGB, including the one in my Fury!

I hedged my bets and ordered a new Power Commander from M&P. On Tuesday evening I directly soldered the Power Commander earth to the engine loom earth. This time it started but there was much popping and farting and spitting back through the throttle bodies. I reckon the device is dead and need to recontact the guy I got it off.

The exhaust secondaries run pretty close under the rear cover and the heat was a bit of a problem, not so much out on track but once you come in and there’s no air flow. The plan had been to insulate it abve the exhaust so I got on with this. I’d got some high temperature contact adhesive from Car builder Solutions which did the job nicely.

The air intake temperature sensor has been dangling in the breeze since reversing the airbox meant the wire wouldn’t reach so I spleced some wire in and got that fitted. i’d been putting off removing the clutch cover – after the fix at Llandow it had been much better but was still seeping a bit. So I jacked up that side of the car to keep the oil over the other side, removed the cover, spent quite a while cleaning up the mating surfaces and the gasket and refitted it with some silicone sealant. Sadly my nice container of Wurth RTV had discharged itself inside the toolbox on the way back on Saturday :( Once that was refitted I ran the engine up to temperature till the fan came on and was pleased to see a nice dry engine and engine bay floor. I then hung around until the fan went off – it’s currently coming on at 92 degrees and going off again at 82 which seems reasonable for now. I can soon tweak it later if need be.

Wednesday evening saw the foam blank for the new seat completed. I then spent ages hacking it to shape – there was loads surplus and the foam adds a surprising amount of weight, it doesn’t seem to expand so much in some places. This ones considerably thinner meaning my bum’s lower and my shoulder blades are right on the bulkhead. Thursday saw it covered in black gaffer tape and refitted to the car. The good/bad news is that it’s 2.5kg lighter than the other one … so even more pies/lead required.

Once that was done I fitted an additional spring to the clutch – Brian had suggested it as the spring inside the slave cylinder is quite strong it will be exerting constant pressure on the clutch release bearing, not a good thing. After loads of unsuccessfully scouring round trying to find one my mate Phil came up trumps with an ideal one from his garage :)

 

Next was the fire extinguisher. I spent ages trying to work out the best place to put it and decided none of them were optimal. I eventually turned it round to find it did in fact fit horizontally immediately in front of where the passenger seat will fit. So after a bit of drilling and more bracket fabrication I ended up with this – it’s a really nice snug fit and the actual cylinder sits between the aluminium bracket and the chassis rail so it’s not tending to roll back and fore with acceleration or braking G forces.

Another blot on the horizon has been getting cold air from the intake in the rear cover to the aperture in the airbox. I ran it temporarily without and it seemed fine but Brian had pointed out that the scrutineers wouldn’t allow it as there are regs about both air filter holes and other holes in bodywork. Ian however said it’s not the case with a rear/mid engined car and indeed the regs refer specifically to front engined cars and to holes in the bodywork “forward of the steering wheel”. Whatever, I want an air duct so I set about making one. As usual I had an ill formed cunning plan and this one involved using PU foam to create a buck for a GRP duct. Here’s a shot of the airbox inside a black bin liner with a cardboard box on top to constrain the foam.

After much cutting and carving, addition of a bit more foam and a 4″ round tube laid up inside a plastic drainpipe I ended up with a GRP moulding that sort of snaps onto the air filter box. Trouble is it didn’t work as planned. I was hoping to attach a flexible hose to it and route this up to the inlet on the rear cover. Trouble is there simply isn’t room, the air filter box is pretty close to the bodywork and there’s no room for the hose. At least now it will be drawing cool air from the intake rather than from behind the engine and close to the exhaust. I think the definitive answer will be a custom airbox but I simply haven’t time for that now :(

Time had gone by exceedingly quickly and it was clear I was going to be pushed to get everything done in time. It took a good couple of hours sorting out the aluminium pipe, routing it, making up brackets for the nozzles in the engine bay and cockpit and connecting it all up. I routed the fire extinguisher cable and got that connected up – I’ve copied what Brian did on their car and routed it across the engine bay and down the nearside sidepod. I then made up a bracket for the cockpit cable and got that fitted. Next job was the external electrical master switch, this is simply a latching push button wired in series with the one on the dash but mounted on the offside sidepod alongside the fire extinguisher pull handle. That way both buttons need to be on for the system to be live. I say simply but the buttons are about £20 each – they’re waterproof and hopefully reliable. Neil C-B had trouble last year with a cheap one cutting out on him.

I bought a pair of universal steering rack gaiters a while ago and it was time to get those fitted – they’re definitely needed for IVA but Brian said the scrutes may well want them also. Simple job but by the time I had the car jacked up, wheels off etc. it was another chunk of time gone. I then got the transponder fitted – this took me a time scratching my head as it’s not so simple to mount as on the Fury as the BDN doesn’t have any open areas in the floor! I assumed it wouldn’t be able to ‘see’ through aluminium sheet but hope it should be OK through the plywood splitter. So I made up a bracket to fit on one of the tubes of the front aluminium frame. I also bolted the horn onto the front bulkhead then wired it and the transponder in and checked they worked OK.

The Fury had a little bracket welded onto the roll cage for the rain light but the BDN doesn’t. I was thinking of making up an aluminium clamp to hold it on but decided I the end to just make a small plate for it to screw on to then fix that to the roll cage with cable ties. It’s very light so they should be quite adequate. I then added a switch to the small dash panel on the driver’s side and got that wired in and tested.

 

The scrutes are apparently very keen on chainguards. It seems to me the only function of the chaingaurd will be to stop the chain wax from flinging off everywhere, I can’t see it doing anything else. First off when a chain snaps it’s apparently fairly undramatic and chains don’t actually go flinging off taking people’s heads off, they usually either just spool off onto the floor or if you’re really unlucky wrap round the front sprocket and wreck your engine. So here’s a shot of the one I made.

 

One of the problems from Llandow was the reverse – despite me being confident it was set up correctly after coming in from the first session the reverse gear was somewhat chewed up. I gather from Brian that he and Ian think the only way it can be happening is through engine mount flex. They’re working on some form of solution but in the meantime I needed to take the gear off and clean up the teeth. I got halfway through this rather tedious job when my weekend was over. I managed to get it finished and the reverse reassembled before work Monday morning.

The number of “absolutely have to be done by the weekend” jobs is now dwindling. Top of the list is getting towing points front and rear, also need to fit the catch tank, the rest are mainly niceties – fitting buttons to the steering wheel to control the dash/logger, fitting some mesh to the rear sidepod ducts, adjust the gear shift leverage, fit the camera etc.

Oh yes!

Well I did get the car out at Llandow on Saturday. There are a few minor issues and it wasn’t really completely finished but overall I’m really pleased.

I was in the garage till late on Thursday night. I got some green paint on the cowl/aeroscreen so that was ready to fit. I refitted the bodywork latches and made a start on making a new foam seat – although the one I made previously looks nice in addition to being too heavy it’s too thick so it pushed me a bit forward and I’m sitting a bit high.

I had the day off on Friday so made an early start. I took the rear panel off and fitted the lights and got them all wired together and connected to the loom via a connector block. I then had a look at the headlights. Once I’d cut a hole for the projector unit the obvious solution was just to simply bolt it in place. I had to nip out for some long enough M5 screws, I also had to hunt around a bit for the festoon bulbs for the combined indicator/side light units. By the time I got back it was lunchtime and it was clear time was going to be very tight. I got all the front lights fitted then got on with wiring them up. This was a bit complex as the projector unit uses a single bulb with a little shutter inside to do the dipped beam. They therefore come with a standard 3 bladed headlight connector, the 3 wires from this then go to a little black box. From this there are a pair of wires to the bulb and a pair of wires that supply the motor or whatever it is. I decided fitting this lot inside the front cover wasn’t a good way to go. So I chopped the wires off and mounted the 2 little modules on my scuttle panel and created a wiring loom running to each unit. This took an age and by the time I’d got that done it was early evening. I could then finally connect up all the lights and check that they worked.

I now realised that there was really no way I was going to get through my to do list – signing on at Llandow the next morning was at 9am and it’s almost an hour away. So I needed to prioritise. Since it was a trackday rather than a test day I decided brake lights were a must so I wired those up and tested them. I also added a couple more batches of foam to the seat. I headed back in at 10pm after a 14+ hour day in the garage completely knackered and more than a little stressed. Brian had rung during the evening to check how I was getting on as he was planning to come down to Llandow if I was going to make it.

I set the alarm for 4am on Saturday and while having my cup of tea sorted out the DigiDash software on my laptop and configured it ready to upload all the settings to the dash unit. I also did the same for the Power Commander and got a reasonable looking map (aftermarket exhaust system and filter) ready to upload, I checked it had mostly positive numbers on it (meaning it was adding fuel rather than leaning it off).

Then it was out to the garage. the seat needed a bit more foam so I did that first. I was keen to have the lambda sensor so I could keep an eye on the AFR so I made up a little dash panel to go to the right of the steering wheel. This, like most of the jobs I’ve been doing, took way longer than it should have. I fitted the brake bias adjuster cable and knob, then fitted the front ARB adjustment rod. I then went back to the seat to find I couldn’t get the darned thing out! Because the upper back part of it was much thinner than the first one it broke up very easily. It was clear there was too much work involved getting this sorted so I reverted to using the earlier version. A simple job like fitting the harnesses and the seat actually ends up taking half an hour or so. At 8 o’clock I was nowhere near ready so I rang Bran to let him know I was going to be late.

I still didn’t have any mirrors so I fitted those. The engine was sounding rough and wouldn’t idle smoothly which I thought was probably fouled plugs the result of too much idling in the garage, they also seem sensitive to starting up with low battery voltage. Sure enough they were in a horrible state so I slapped new plugs in and she sounded much happier.

I decided then that everything else on the todo list was staying there. Before loading her onto the trailer I quickly threw her onto the scales and set the corner weights. Then it was on to the trailer to discover that the wheel chocks at the front were too high to go under the splitter, and of course one of the bolts was seized. So I had to find the angle grinder, stick a cutting disk in it and cut that off! By the time I’d loaded all the tools into the car, got changed, found my overalls and helmet it was about 10 o’clock. By the time David and I set off I was feeling frazzled and more badly prepared for any trackday I’ve every done :( I’d decided though that just getting in the car and driving it round a few laps to see if everything worked OK was the priority.

On the plus side it was a beautiful day. Llandow, like most circuits always seems to be cold but there was no wind and it was t-shirt weather. Brian was there when we arrived and was chatting to Darcy Smith who’s well known to the RGB paddock. We got the car off the trailer and I tightened up the locknuts on the suspension pullrods, rear toe adjusters and the track rods. After sticking some fuel in I got changed and headed out onto the track. Although my driving position was a bit compromised I soon found that I was OK in there. Everything seemed fine and the first impression was of how smooth the car was, largely a result of the chain drive without the backlash of the diff but partly also no doubt due to the suspension being in a different league to the Fury. The brakes felt fine, of course the pads were brand new, I was on brand new tyres so I was taking it pretty carefully. The biggest problem was the gear change, I missed gears a few times due to the imprecision of the shift, I was having to pull quite hard on the paddles. The throttle pedal is also very different to the Fury with its rising rate cam action and I was surprised how effective it was. After a couple of laps I went a little bit quicker. I’ve no idea how much quicker as I didn’t have a functioning speedo and therefore no gear indicator either. The engine was revving out nicely but with a slight flat spot around 7-8k, it sounds very different to the Suzuki and in fact sounds more like I remember the ZX12 in the BDN David Wale is now driving. Of course the engine’s only a few inches behind my head so I was hearing mainly mechanical engine noise rather than the exhaust. I’d been expecting it to have a strong top end but to be relatively weak low down but to be honest it didn’t really feel down on torque compared to the Fury, of course the significantly lower weigh will account for some of that.

So, what’s it like to drive? The handling was a revelation, the steering action’s of course very quick but the car isn’t the least bit twitchy and feels much more stable than the Fury. The main thing was the feel and feedback from the car, I was surprised how much confidence I got in it from the off. It was also very stable under braking and the braking was immense. I had the bias deliberately set well forward and didn’t take it to the point of locking up at any stage, it was a dry sunny day and Llandow is a very high friction surface. There are also a lot of ripples in one of the 2 main braking zones so it’s not a good place to play with that. I was of course well aware of the potential risks with a mid engined car but found the car reassuringly easy to catch when I did step the back end out.

After a few laps I went back in with a huge grin. There’s something very special about your first time out in a car you’ve built yourself. Brian was keen to hear how it felt and I think was relieved that I was so pleased. Water temp was in the 60′s, oil temp just up to 80 degrees so all was looking good on that front. Oil pressure at idle was even more crap than the Hayabusa at 4psi! Normal for a Kawasaki according to Brian. Oil pressure on track seemed fine, not dropping below 60 when I looked at it round the longest right hander. The DigiDash warning was set for 30psi and never made an appearance so all seems well on that front.

There was a bit of oil in the engine bay – I’d had a slight leak from the clutch cover when I’d got the engine up to temp before and of course hadn’t had time in the last frantic week to sort it out, so I took the cover off and refitted it with some RTV. It was really helpful having Brian there having a look around the car and I was very grateful to him making the effort to give up his time and come over for the day. Ian was up north doing recovery vehicle duties on a rally. We also had a good look at the gear shift cable and linkages and identified no issues, the routing of the cable looks fine and we concluded the difficulty was just inherent with a 3 metre cable. Brian’s planning a centre mounted stick on Rob’s car with a link running directly back into the engine bay and I might investigate this further.

I did about 5 sessions in all by which time I’d achieved the aim of the shakedown, I also had no neck muscles left partly because I’m an unfit slob but partly because I’d never had time to fit the aeroscreen. So, I’ve no idea how fast I was going, I’ve got no data logs and no on board video but the car works. There are some issues to sort but I now know I’ll have a car to race at Mallory in a fortnight.

What did surprise me was that both Brian and David said it was very quiet, with other cars on track they couldn’t hear me on the other side of the track which is only about 300 yards away. I’m pleased about that, apart from getting through scrutineering without needing to worry it means I’ll be able to take the car on trackdays at some of the more noise restricted circuits.

So at about 4 o’clock we loaded her back on the trailer and headed home. I felt a whole heap more relaxed driving back than I had on the way there but I was completely knackered. I got home, stuck the BDN in the garage, left all the tools and stuff in the car and shower and a quick beer and curry excursion with Jen was in bed by 9.

Midnight Oil

After 3 days torturing GP trainees in Croydon I returned to an overnight shift on Saturday night :-( After no sleep I managed to stay awake all the way up to Brian’s and home again on Sunday with the collection of parts shown in the pic to the right – rear finisher panel, splitter, aeroscreen moulding and a couple more laser cut aluminium parts to mount the splitter and beef up the rear undertray.

I got the rear panel and aeroscreen trimmed then set about getting the panel to fit. This involved quite a bit of work including trimming the back of the rear cover so they fit together snugly. It’s impossible to completely cover the hinge and its bolts but I was really happy with the overall appearance. I then spent a while with hot soapy water and wet and dry getting it ready for some paint, Brian had used some different wax and it proved fairly tenacious. Once that was done I set the garage up for spraying again and gave both parts a coat of primer. By now it was 5pm so I headed off to the pub with Jen before I fell asleep in the garage! At this stage I was feeling a bit overwhelmed with the amount of stuff I need to get done if I’m to make it to Llandow next Saturday.

After a nice undisturbed night in my own bed I got up at 6am and started preparing the headlight pods. The black parts need to be bonded under the front bodywork in exactly the right position without much margin for error. So my cunning plan involved masking the edges of the covers so they don’t get sealant on them then temporarily sticking them onto the pods using a few bits of double sided tape. Once that was done I headed out to the garage and rubbed down the rear panel and aeroscreen, then hung up my tarpaulins and polythene sheeting ready for painting in the evening.

At lunchtime I went shopping for a few bits and pieces – some 12mm marine ply for a spacer for the splitter, some aluminium angle for setting up the geometry (I chopped up my one of my old ones to use them for bracketry for the exhaust heat shield!) and some fairly heavy duty steel angles to bend the undertray/splitter brackets.

First job on Monday evening was spraying the 2 parts. This was going OK until I got a couple of runs – the problem is that the rear panel has quite deep recesses for the light units and when you spray these recesses they accumulate paint so as you spray the surrounding area it’s all too easy for the paint to accumulate to the point that it runs. It’s no disaster, once it’s properly hardened I can rub the runs down. I’m also mindful of the criteria for acceptability of paintwork on a racing car, there’s really no need for it to be concours standard.

 

And here’s the aeroscreen, I’ve painted it white but I think it may well end up green :)

 

With that done I then got the undertray support brackets bent, then decided to have a look at the rear spoiler. Clive wasn’t able to do all the bending of this – the rear edge drops down at 90° then needed to be bent around in a radius. Brian supplied 2 little turned aluminium bobbins to go in the ends, the screws then go through the brackets and into these bobbins to hold the rear edge. Fortunately I had a length of aluminium bar exactly the same diameter as the bobbins so I used this as a former to bend the edge around. Sounds simple but actually took quite a time. Once it was done I bonded the bobbins in the ends and clamped them up.

Next on the agenda was bonding the headlight pods into the front cover. This went fairly well, the left one needed a prop to keep it pushed into position but the right one just stuck straight into place. While they were drying I cut the strip of 12mm marine ply to act as a spacer for the splitter then sanded it and the splitter down and drilled the holes in the spacer. Then it was time for bed!

On Tuesday morning I turned the cover over to remove the headlight covers. I’d wondered if this might be difficult but I’d only tacked them on with little squares of double sided tape and they were fairly easy to remove. I then trimmed away the excess PU sealant, removed the masking tape from the covers and checked the fit. Very pleased, they look really great. Just need to work out how I’m going to mount the headlights now …

Next I turned my attention to mounting the rear panel onto the aluminium frame. I really wanted to conceal the bolts so I went for one in the centre of each stop/tail/indicator recess and one each side of the number plate recess. The trouble is that the LED lights don’t come apart like ‘normal’ lights and are intended to be retained by self tappers into the back. So what I planned to do was stick 6mm roofing bolts (which have a nice shallow head) with a big repair washer on each side of the GRP and a nut on the back so they act as captive bolts. The panel needs to be spaced off the aluminium frame anyway so the nut and washer behind the panel are no problem. It didn’t take long to get the holes marked and drilled, the bolts installed and it was a nice fit.

The lower edge of the rear panel at the sides is designed to fit just flush with the edge of the undertray, so the next job was to remove the rear cover and get the undertray support bracket fitted and drill some holes in the flange along the side of the undertray to bolt through it into the rear panel. On Tuesday evening I got some holes drilled to fix the rear panel to the edges of the undertray. The splitter also got a coat of black paint.

I decided to slap the spoiler on next. This turned out to be pretty easy, just requiring the M6 screw at each end then a series of holes for M6 screws along the lower flange. Brian had suggested going for maximum downforce to make it as un-tailhappy as possible but at the uppermost position it really looked a bit too jaunty so I stuck it down 2 holes. It had got a bit marked up while I’d been doing the forming of the rear radius so it got a bit of polishing next :)

Early on Wednesday I took the bodywork off and made a start on the geometry. Once I’d got my pair of aluminium angles marked up symmetrically I clamped them to the chassis and set up the string lines. With my 90 kilos of sand in my seat I set the ride height which was a doddle because of the nice turnbuckle style pushrods. On the Fury setting up the camber and wheel alignment used to take an age – undoing wishbone bolts, adjusting rose joints then doing it all up again, making sure the spacing washers were in the correct places etc.On the BDN it’s just a simple matter of turning the track rods at the front and the upper wishbone turnbuckle rod at the rear. The camber’s already set by the shims on the uprights so I didn’t need to worry about that. I had the whole lot done in about an hour.

I then got the front splitter fitted onto the front of the car. Before I could refit the bodywork I needed to run the wiring harness for the rear lights down the sidepod, in this case just a length of 7 way trailer wire. I then ran the lambda sensor wire down the driver’s side. With those done I could start refitting the body. I discovered the front cover was a whole heap more difficult to fit as the splitter makes access to the bolts more or less impossible with the cover down so I enlisted the help of David to hold it upright while I refitted the bolts. The sidepods went on nice and easily followed by the rear cover and finisher panel. Then it was time to wheel her out of the garage into the sunshine.

Of course it helps that it’s a nice sunny day but to say I’m pleased would be a bit of an understatement :D I only had time to take a few shots then (using the functioning reverse!!) reverse her back indoors as I had to head back to work. There’s a break in hostilities now as I head off to Croydon again this evening but only for a day, back on Thursday evening. Still a lot of work to do – you’ll notice there are no lights yet, also the lambda needs fitting, I need a small dash panel fitting to the right of the steering wheel and quite a few little jobs to sort but I think it should be doable by Saturday.

Here’s a closer view of the front corner. I’m really pleased with the headlight pods, the cover’s only resting in place here. Fitting the combined indicator/side light will be a doddle but the projector dip/main will be a bit more challenging. For race use of course it doesn’t really matter which way they point so I might just get them screwed in however I can until it comes time to make them adjustable for IVA. I’ll then probably use double sided tape for the covers.

 

You can see the spoiler in this shot. Hopefully it won’t upset Mr. IVA too much – their main concern is sharp edges and of course the rear of the actual plane is radiused anyway, I might need to stick some trim strip around the brackets, they’re probably too thin to be able to round them off to the required radius.

 

No lights yet but I’m not anticipating huge problems getting those fitted. When I went up to Hereford a couple of weeks ago I took the light units I’d bought and Ian measured them all so they should be a pretty good fit in the recesses.

 

For now the bodywork’s just slapped on, all the fittings allow a little adjustment so I can tweak it to improve some of the shut lines although to be honest it’s not looking too bad as it is. Now, where’s that can of green paint …

Running out of time

On Monday evening I didn’t get long in the garage. Over the weekend I’d tried reversing the car without a lot of success – there was a lot of chatter and it was dropping the battery voltage enough to cause the electronic cutoff solenoid to cut the power (it needs 12v across its terminals to keep it switched on). So I dismantled the reverse mechanism to adjust it as I suspected the motor was a bit too close to the reverse gear and there was no more adjustment left. It took a while but eventually I had it back together again to discover that the battery voltage was low to start with – just having the solenoid powered up seems to drain it. So I stuck it on charge and left it for the night.

On Tuesday evening I decided it was time to tackle the undertrays. The rear one actually took me less time to fit than I expected, just requiring the removal of a couple of chassis bolts which hold it on followed by 4 M6 screws into the rear aluminium sub-frame. It’s nearly as smart as the one I made for the Fury ;)

 

And here’s another view of the rear sub-frame. the front took a little longer to fit because … wait for it … Ian had dropped a small clanger and got some of the mounting holes in the wrong position. He had warned me about it and is getting a new one from the laser cutters, but it’s a very minor problem and I decided to go ahead with the one I have and measured up and drilled some new holes in it.

 

I then redirected my attention back to the throttle pedal and cable. I wasted quite a while rummaging round in my various boxes of bits looking for the return spring Brian supplied before deciding it had to have rolled under the driver’s floor panel. After undoing the dozen or so self-tappers it was indeed there and after a quick phone call to Brian followed by an emailed photo back I had just about worked out exactly where it went when it was time to head in.

The first race weekend is now less than 4 weeks away. My plan was to go to Llandow testing so I rang to see if I could go on Friday the 18th but apparently 5th Gear have an exclusive booking for the circuit for the day. They did however offer me a place on their trackday on the Saturday, these are usually initially sessioned followed by open pit lane and they said they plan a couple of test sessions during the day so I thought that sounded a reasonable plan and even cheaper than their testing at a very reasonable £90 for the day. It’s not about finding speed, I just want to have a shakedown and make sure everything’s working OK, keep an eye on the oil pressure and air/fuel ratio on the logger, set up the brake bias etc. and generally get a bit used to the feel of the car.

On Wednesday morning before work I got the throttle return spring fitted and made up a new cable. The one from CBS is actually a bit heavier duty and certainly feels better than the previous one I made up. However it just took quite a while making it up and by the time that was done it was time to go back in. That’s now it for this week really as I’m back in Croydon until Saturday evening. I’m then working overnight Saturday and heading up to Hereford Sunday morning to get the rear panel and the splitter from Brian. I then need to try to get everything done to take the car on track within the following 5 days. Starting to feel a bit of pressure now.

Before hitting the M4 on Wednesday evening I managed to give the credit card a bit of a mauling by ringing Demon Tweeks and ordering mirrors, harness and a few other bits and pieces including the HANS device I’ve been planning to get for ages.

Painting the bodywork

I made an early start on Friday although it was b****y freezing! progress was hampered a bit as the Fury needed a bit of attention. Following a query by someone looking for a FuryBusa I’ve been in email negotiations with someone in Sweden who’s keen on it and is supposed to be coming over on on Saturday to buy it. It hasn’t moved since I parked it in the garage after Silverstone, apart from the faulty Power Commander it’s pretty much good to go but needs a good clean and checking over.

Having prepped the front cover the day before I did the same for the rear cover and the offside sidepod. I left the nearside sidepod for a while as it needs more work for access to the fuel filler. Interlink arrived early with the parts from Car Builder Solutions – a lockable flush mounting filler cap, some 2″ flexible hose, a 2″ to 1.5″ reducer and some clips. With the Fury and the BDN outside sunbathing I got the garage ready for some painting – a general tidy, some sweeping and screening off the far end with a couple of tarpaulins. With the front and rear cover and the sidepod resting on a variety of trestles, chairs etc. I gave them a wipe over with a cloth and some cellulose thinners then again with tack rags.

Actually spraying the primer took a surprisingly long time as the 2 main covers represent a significant surface area and the fairly deep valleys inboard of the wheel arches took a time to get a good covering on them. Once that was done I got going on the Fury, giving it a good wash and getting all the bits of tyre rubber from Silverstone out of there. She started first turn of course despite having been sitting for over 4 months. I also rewelded a new lug for the front ARB onto the wishbone as that had become detached at Silverstone.

By the time I’d finished with the Fury and got the tools away the primer was dry so I did a repeat of the rubbing down operation on the 3 panels but this time with 600 grade wet and dry. There are a few areas with little pin holes particularly along where the mould seams were and I may well give them a bit of filler and some more primer before spraying the topcoat although it’s possible the topcoat would fill them.

Another frosty start on Saturday morning. After slapping a bit of filler on the tiny defects in the front and rear covers I turned my attention to the fuel filler. This has been another of those problems that has been on the horizon that I had never really mentally resolved. IVA is the problem of course – the standard BDN arrangement is with the filler cap located in the tank top cover but IVA doesn’t allow the fuel filler to be in the engine bay. Stick it on the outside I hear you say … but racing regs say you can’t have the fuel filler cap outside the bodywork or likely to be damaged in a crash, and having it sit on the outside of the sidepod would be risky. Space in the top corner of the engine bay is extremely tight so getting the position right is critically important. On first glance the gear cable appeared to be the fly in the ointment but in fact it turned out not to be since the filler can only go so far into the corner anyway and there’s still room for the cable to squeeze through. I made a start by cutting out a little aluminium panel to fix to the chassis. After a bit of cutting, filing, bending and drilling etc. here’s what I ended up with. Pretty pleased.

Now I had to work out how I was going to create a tidy looking recess in the sidepod so I could get at it without removing the sidepod. As usual a cunning plan came into my head. What I wanted was a slightly tapering recess which at the inboard end was just about the same size as the filler cap surround but was a bit bigger at the outboard end to make access easier. Among my various empty containers in the garage I found a plastic pot that looked about right. After a bit of cutting and filing it sat nicely on the inside of the sidepod and I then laid up some of the very lightweight fibreglass mat and resin to create my recess.

While this was going off I touched up the primer on the front and rear covers. I wanted to round the edges of the recess so I added a thick fillet of glass reinforced filler around the base of it and left that to go off while I carried on getting the Fury and the spare parts for it ready. When I came back to it I used the Dremel sanding drum to sand away the rim of GRP on the outside which then allowed me to fairly simply pull the plastic pot out – it was a sort of polythene material and the resin hadn’t stuck to it.

What I needed to do next was trim it back so it fitted just shy of the filler cap and this bit I messed up by cutting it a bit too short meaning I had to build it back up with filler. This took a couple of applications but in the end I had it the right size and shape with a few imperfections. Meanwhile Fredrik arrived late afternoon and collected the Fury, my last job of the day was then to sand the recess down and add another layer of filler to it. I know this is all sounding pretty terrible but I reckon the final result will be fine :)

On Sunday morning I finished off the filler recess and then got going prepping the front and rear covers for topcoat and the nearside sidepod for primer. When I came to paint the covers my spray gun was playing games and made a bit of a mess of it, I couldn’t get it to spray in a useful pattern, it was spraying a sort of fan but with more paint at the ends of the fan than in the middle. It wasn’t all down to the gun though, despite spending ages prepping the panels there were lots of little dark spots on them, especially the rear cover. I’m not sure whether it’s tiny bits of oil coming through from the compressor or some remnants of grease or wax on the panels themselves. It then took ages for them to dry and harden off for me to rub the dodgy bits back.

While I was waiting for paint to dry I got the oil cooler sorted out, it had been temporarily swung round into the engine bay to keep it out of the way. I turned some small aluminium bushes to space the slight gap at the top mounts and bolted it into its housing. I then left the housing floating free until the sidepod it fitted, it’ll then bolt onto both the chassis and the sidepod floor.

I managed to get the sidepods primed, rubbed back and a few defects in the primer touched up again and by mid afternoon I was ready to give all the panels a layer of topcoat. I used my smaller touch up gun this time and it worked much better. While they were drying I got on with the fuel filler. The tank cover that’s on the car has a 12cm diameter hole in it where the filler neck is welded in on the race car so I made up a plate to fit over this and made a hole to take the 2″ to 1.5″ reducer. Once that was done I cut the respective hoses to length and fitted the assembly. It works rather well, all I need to do now is seal around the reducer with some PU sealant and wrap the upper hose with some of the reflective matting.

Definitely in sight of the finish line now. The paint on the bodywork needs some cutting back but that can be done once it’s fitted. I can also finish off the electrics – fit the headlight pods, rain light, front and rear lighting looms, horn, transponder, speedo sender, GPS antenna etc. There’s also a small oil leak from around the clutch cover somewhere that I need to investigate. I also need to get the rear finishing panel from Brian as soon as it’s done and get it painted and fitted and the rear lights mounted onto it.

End of an era

I never did get around to advertising the Fury. Initially I was hanging on until I could be confident the BDN would be ready in time for the start of the season but more lately it’s been more of a case of not getting round to it. Anyway a week ago yesterday a message was posted in the BEC Yahoo Group on behalf of someone in Sweden looking specifically for a FuryBusa to race.

So I had quite a bit of email correspondence with Fredrik in Sweden who was of course able to discover anything he wanted about the car via my blog. We agreed the sale and he came over to collect it yesterday! He’ll be racing it in the Swedish ModSport Series where his main competition will be car engined Sevens. Having driven 2,000km to get here he was in a bit of a hurry to get away as he needed to get back home by Sunday evening!

It was sad to see the car go, she’s been a big part of my life for the last 4 years or so and although we had our ups and downs together the 2010 season was pretty good. Having the cash helps of course and it’ll give me lots more room in the garage.

More pies required

I’d hoped to get loads done on Wednesday but it didn’t go to plan. I decided to nip over to see Clive the aluminium fabricator and sure enough he has a folding machine and was happy to fold my undertrays for me, so I left them with him. He didn’t have any suitable offcuts of round steel bar but he did have some 40mm x 20mm flat bar and let me have a length of that. So instead of going to the gym I hacksawed a couple of chunks off that to make my thrust washers for the drive shafts as in this photo. Here I hit my first problem. I knew my lathe had an additional 4 jaw chuck with it which I thought would come in handy for this but when I took the 3 jaw chuck off I discovered that the back plate is only drilled for 3 mounting bolts and the 4 jaw chuck has 4. So I had to hack my lumps of steel with the hacksaw into something I could roughly centre in the 3 jaw chuck. The next problem was that the normal jaws won’t hold a 40mm round piece and I had to use the bigger ones which meant that with a piece only 20mm thick I could only get at the last 8mm or so. So it took me ages of faffing to get to a round blank.

And then I had to stick a 20mm hole in it. Easy up to 10mm just using drills. But then I wasted ages trying to enlarge the hole with the boring bar that came with my set of Glanze tools. After lots of frustration I realised that although all the other tools in the set are at the correct height when just mounted onto the tool holder the boring bar is set too low. Once I’d packed it up with a shim it actually started cutting the metal correctly and I could get my washers completed. I then got them fitted and the hub nuts torqued up with my shiny new breaker bar and some split pins in. Then it was time to nip up to get the undertrays back from Clive.

I’d made a start packing the diff with grease the other day but my grease gun was empty as was the tin of grease I had so on my way to Clive’s in the morning I’d got some more at the motor factors. Once I’d got grease all over myself packing the grease gun I got going. The diff has about 6 grease nipples on it so as advised by Brian I removed one and filled it from the other side. I was pumping grease in for what seemed like ages and felt like I seemed to be getting nowhere but then the grease gun was empty and I realised the diff just takes a lot of grease. After refilling it and a bit more pumping I eventually got some oozing out of the hole on the opposite side then I went round the other grease nipples until the whole thing was full.

With that done I decided to fit the front stub axles next. The front hubs are identical to the rears but of course don’t have a drive shaft to hold the hub together, so Brian’s supplied me with a pair of stub axles, basically I think he’s butchered a pair of CV joints and machined a flat face on the ‘back’ of the spline. This looked a pretty easy job and I didn’t expect it to take long. But it did :( I tried to do the first one up and the shaft was just spinning (it’s a smaller diameter shaft than the rear so it just sits in the hole without the splines engaging) with no easy way to hold it. After a few goes I realised that the spline was just a bit longer than the width of the hub so the thrust washer was seating on the shaft and the nut tightening on it before it actually clamped the hub. So, back to the lathe to machine a small recess in the washer to allow it to seat on the hub. Next problem was that the washer wasn’t thick enough, but with both washers fitted on one side it was fine. I then ran out of time as I had a retirement do to go to so first job on Thursday morning was going to be hacking another lump of steel into shape for a washer for the other side.

Thursday was a much more productive day. It still took a while turning the thrust washer but no drama and I had it done and the stub axle fitted by 10am. My mate Phil came round for a nosey and gave me a hand with something I’d been looking forward to doing for some time – sticking her on the scales. So we jacked her up, connected up the plates and zeroed the scale then lowered her onto the plates. The moment of truth … 427.5 kilos :D Of course there are more things to be added to the car but nothing of any substantial weight – lights, rear trim panel, seat and harness, undertrays, fire extinguisher. Even allowing 17.5 kilos for these plus say 95 kilos for me in race suit with helmet leaves us at 540kg, 20 kilos below the minimum weight of 560kg for Class R in RGB. More pies then.

Once that was done I made a start on the headlight housings. These are a black plastic base moulding that fits under the wheel arch with a clear plastic cover that sits on top of the base and is a snug fit inside the hole in the GRP. So the cover is used as a template to cut the hole. After covering the left hand wheel arch with masking tape I worked out where I wanted it – the critical dimension is having the dipped beam cut-off a minimum of 500mm from the ground. Looking at the drawing Ian had provided he has the pod positioned so that the top of it is just below the top of the wheel arch, i.e. it doesn’t protrude up above it. So with a spirit level resting on top of the highest point of the wheel arch I slid the pod backwards until it just touched the level and marked this point. I then did some measuring to get it in the centreline of the nacelle down at the front. Once I was happy with the position I measured up and marked up the offside to match then marked the outline of the cover on each side.

After much checking it was time to take a deep breath and set to with the cutting disk in the die grinder which rapidly resulted in a large hole in the panel. I then tidied up the edges with the sanding drum and some wet and dry and confirmed that the light pod fitted nicely then it was on to the other side.

 

And here’s a shot of the whole headlight pod taped in position.

 

Before taking the bodywork off I marked up the rear face of the front cover which will be the dash area as it needed a couple of cutouts – one on the left for the switch panel, one in the middle for the DigiDash wires to come through and one on the right for a couple more switches and the lambda gauge. After cutting these out and checking I could get at the switches OK without the opening being too big (this should avoid the IVA tester’s sphere of doom coming into contact with anything sharp) I got the bodywork off and stuck it outside in the sunshine.

Time now to have a quick gander at the clutch – the system is bled and functioning but I hadn’t done any adjustment so far, so I stuck the seat in and started her up to try it out. And it worked nicely although the bite point was with the pedal quite a way off the bulkhead so I screwed the pushrod further into the clevis to effectively shorten it which put the bite point a bit closer to the bulkhead. This means firstly that the clutch arm isn’t being pushed too far (which isn’t a good thing) and secondly it maximises the disengagement of the pushrod so it won’t tend to make the clutch slip. It worked very nicely and I was able to select first gear and creep the car forwards in the garage then drop it back into neutral.

By now it was late afternoon. It was a nice sunny day so I made a start on prepping the bodywork outside, starting with the front cover. Once I’d tidied up the dash apertures I started rubbing down the surfaces to be painted. The front cover has a flash line from the mould running longitudinally down each wheel arch so I flatted those off then went over the whole panel with some 400 grade wet and dry with plenty of warm soapy water to both flatten it off and remove the residual wax from the mould. This actually took quite a while as its a fairly big panel and I wanted to get it right. By the time that was done it was time to clear up and head in.

Completely Exhausted

With the car dropped off at Pro-Speed in Cardiff I headed home and gave the garage a tidy, it’s surprising how much easier it is without the car in the way. Sure enough Charlie rang me mid-afternoon to check it was OK to pick the car up in the morning which seemed very reasonable seeing as he’d lost an hour and a half this morning through me being late. Apart from tidying up (the bench is still completely cluttered) I can’t get on with anything BDN related until the car comes back.

One thing I forgot in the last blog entry was that I fitted the drive shafts on Sunday. This turned out to be initially much easier than I’d expected, I just undid the top 2 bolts on the upright, hinged the upright down, pushed the drive shaft into the diff, a couple of taps with the rubber hammer then fitted the other end in the upright and replace the 2 bolts. Then it got more interesting – there’s an awful lot of thread on the end of the shafts and unlike the Ford shafts I’ve been used to these shafts are drilled for a split pin and come with a castellated nut. The trouble was it looks like they need a very thick (maybe as much as 10mm) thrust washer and none were supplied with the shafts. It looks like Tim Hoverd had the same problem and machined up a pair. I don’t have a large enough piece of steel bar so I need to either find some bar or see if the Vauxhall dealer can get me some washers in, they must be a standard part. In the meantime I can’t actually do up the nuts very tight as they’re so far on the shaft that my socket won’t reach them.

Another job on the to do list is folding the undertrays. These are laser cut aluminium and need some quite long folds in then. My mate Phil thinks someone round the corner has a folding machine so in preparation I got the undertrays in the nice warm kitchen and measured/marked them all up.

While I was twiddling my thumbs waiting to go to collect the car I decided to have a look at the battery booster pack I got from Halfords some time ago. It was something like 25% off and has a 20AH battery but it’s never actually worked properly – all the bits like the compressor, light, AC inverter etc. work great but the jump leads never had. Trouble is it’s trying to be too clever. It doesn’t do anything till it detects that the leads are plugged in, then it doesn’t make them live unless it’s happy they’re connected with the correct polarity. I pulled it apart and there was nothing obvious wrong, no leads disconnected etc. so I decided it was the little circuit board that does the decision-making that was at fault. It turned out to be pretty simple to make it a whole lot stupider just by connecting the lead going to the jump lead socket direct to the 12V post bypassing the circuit board. Job done :) Mental note to self to try to remember to connect them the right way round when I use them …. drrrrrrrrr

I got over to Cardiff to find Charlie still quite a way from finishing the exhaust. He’s a busy boy and since he does all the critical work himself he gets delayed every time he has to speak to someone on the phone. Space under the rear cover is pretty limited. Because the primary and secondary lengths Tony gave me are quite long (about twice as long as most systems) that meant by the time the cat was in there we were already quite a long way back in the engine bay. When I got there he had the system made and in place and was sorting out some brackets to hold it. So I toddled off to Machine Mart which was just round the corner and got myself a 1/2″ drive breaker bar ready for doing up the drive shaft nuts.

By the time I got back it was nearly done. Charlie’s workshop is quite amazing, the amount of stock there, miles of stainless tubing in all diameters up to some huge stuff that must be 150mm or so in diameter. Also loads of ready formed bends, tailpipe ends, silencer box end plates etc. Here’s a shot of the roll of silencer wadding – us RGB boys usually pay up to about £30 for a metre of this stuff, the roll in the photo is about a metre wide. Incidentally my silencer isn’t repackable. I did encourage Charlie to make it packable but he is confident there’s no need. He reckons our exhausts blow the wadding out because we don’t pack them properly, specifically without enough wire wool around the perforated tube. He reckons with a double layer of wire wool the hot gases don’t actually get to the wadding. We’ll see, I’ve no doubt he’ll sort it if it does turn out to be an issue.

Anyway, here’s a photo of the completed work of art. Again it’s all in stainless and looks beautiful. As soon as Charlie had finished the system we reconnected the ECU and started her up. I’d been encouraging him to use as big a silencer as he could fit in there but I accepted that he knows what he’s doing and left it to him. I was very impressed, it’s really quiet, most of the noise I could hear was the mechanical engine noise until it’s revved quite high. The proof of the pudding will be in the first noise test of course but I’m pretty confident it will be fine.

And here’s another photo from the side. The drawback with this system is that it puts more weight on the rear aluminium subframe, although there is a bracket welded onto the main subframe just where the main pipe drops down after the cat. I’ll just have to keep an eye on it.

 

Once I got the car home I had another go at getting a photo of her out in the daylight. As Dave commented on my previous posts photographing white cars especially in sunlight isn’t easy but here you go. I think she looks fantastic! She’s a tight squeeze on the trailer and I can’t use the usual tie down holes in the trailer floor as they’re obscured by the sidepod floors.

Once I got her back in the garage I got on with finishing off mounting the sidepods – bonding the mounting plates at the rear end along with rivnutting the chassis to take them, also turning down acetal bushes to space the sidepods from the front chassis mounts. I also added a rivnut for the oil cooler housing. And that was the end of the day’s play.