Monthly Archives: August 2011

Making space in the garage

On Monday evening I made a bit more progress. The steering rack first – I replaced the threaded part on the end which took only a couple of minutes, remove split pin, unscrew end cap, fit new part with a bit of grease, screw end cap back on and refit split pin. Another job that had been on my to do list prior to the crash was to adjust the rack, it had a tiny bit of play in it. On the Titan rack you just undo 4 (imperial!) allen screws and turn a slightly eccentric cam then tighten the screws again. It took all of two minutes – if I’d known it was as easy as that I could have done it in situ before!

I then removed all the bolts from the pedal box and cleaned them up along with the steering column, steering UJ and its associated bolts and after a bit of degreasing they got a coat of the Trimagard paint. They got barbecued in the evening and on Tuesday morning I bolted the pedal assembly back together. The angle bracket that holds the gear shift cable outer on the upper steering column assembly had got bent which I think accounted for my sore right knee, so I stripped that down, straightened it and cleaned it and its bolts up then bolted it onto the chassis.

Tuesday evening saw the nice shiny steering column fitted. With the UJs fitted in phase with each other and all the bolts tightened up the steering had a nice smooth feel with no hint of play. I then just had to fit a couple of rivnuts to the new chassis rails to bolt on the aluminium angle that supports the upper column.

I then moved onto the brake pipes, refitting the short sections that cross the chassis front and rear. I could then fit some new double clips and make up a new rear brake line. On Wednesday morning I got the clutch line done. I also cleaned up the ARB and painted its bolts and stuck them in the oven.

Wednesday evening saw the ARB and the cockpit adjuster refitted. I then refitted the hydraulic fluid reservoir and connected the reservoir hoses onto the master cylinders. I figured it was now time to drop the car off the trestles it’s been sitting on as it’s too high for engine installation. So using the engine hoist to support the rear end I lowered it down onto a pair of timber spars resting on axle stands.

I nipped round to see Clive, the local fabricator I use and dropped off a few parts for him to fettle. I’d never got round to getting my fuel tank filler pip welded into the tank cover so I took that, also the exhaust manifold, one of the welds holding a small bridging piece between the 2 secondary pipes had let go. I also took the new laser cut front undertray parts and their respective drawings for Clive to fold them. I could do them myself but the bigger one needs all 4 edges folding and would be pretty tricky using my angle irons and hammer. Clive’s workshop is a few miles away near Ammandford but he lives in my village and he rang me on Thursday afternoon to say the parts were all done and I could pick them up from the house in the evening.

Quite a bit of ordering has gone on – some new bolts from Namrick, headlights from Russ at Furore who was kind enough to take pity on me and do me a deal, replacement front side/indicator lamps from Car Builder Solutions. I’ve also ordered a brake pressure transducer from Ebay and a bunch of fittings to graft it into the braking system. 4 new tyres arrived from George Polley last Friday.

With the car a bit lower I bolted in the lead ballast then refitted the newly welded up fuel tank cover with the filler hose adapter welded into it. I also refitted the coolant swirl pot.

 

It was now time for an engine so I got it cleaned up and hoisted that back into the engine bay and bolted it in. This was all actually pretty undramatic and pretty soon I had the engine secured and could get on with bolting the manifold back onto it. Once that was done I refitted the coolant hoses and the front engine stays. I’d also fettled the reverse gear – the new gear had become quite badly chewed up despite the modified engine mounts. We now think we know why – Ian had been talking to Andy Bates who reckoned it’s not due to engine movement within the mounts (indeed I’d had trouble comprehending how this could happen) but due to a combination of the gearbox output shaft flexing and the engine casing distorting under load. Yes, really. I gather Andy got his information from Powertec. So the answer is to weld up the output pinion on the reverse starter motor and grind the end off the shaft so that even when the gearbox output shaft migrates backwards it doesn’t impinge on the pinion.

Refitting the radiators was only a 10 minute job. I then refitted the fire extinguisher. For a while I’d had it in mind to delay racing till I’d IVA’d the car but with the IVA inspector being away and me also being away for a few days early in September it would effectively have meant missing both Oulton Park and Pembrey. Jen thought it made more sense to concentrate on getting the car back out racing and forget about IVA until the end of the season so I’ve gone with that. By now I could see a bit more of the garage floor as the piles of bits got gradually smaller.

I spoke to Rimstock late in the week to check on progress only to find that they’d cocked up and having initially raised the order then cancelled it, so no progress on my wheels. I politely expressed my disappointment and explained the situation and the chap I spoke to said he’d do what he could to get them sorted ASAP. I’ll call them on Tuesday to give them a little gee up.

On Saturday I nipped up to Hereford to collect bits from Brian. He hadn’t expected to be able to sort my front sub-frame until next week – as soon as he cut tubes out of the old one it sprang into fairly inappropriate shapes so a whole new one needed to be made and Bob at Concept Racing had a backlog after returning to work from his latest surgery. So I was a bit surprised when Brian came out of his workshop holding a shiny new freshly TIG welded sub-frame – apparently Bob had got it done on Friday afternoon. Brian had also been busy and sorted out my replacement aluminium parts – pullrods, steering rod, suspension mount and the diff carrier. He’d also laid up a pair of new sidepod floors. He already had a pair of sidepods there intended for his son Rob’s car but they’re outsourced anyway so not a problem for him to replace those. I’m feeling a bit guilty about the number of parts I’ve pilfered that were originally for Rob’s car!

Brian also had a look at my nearside drive shaft. When I’d removed it it felt as though the shaft was pulling out of the inner CV joint. I didn’t try pulling on it again as I didn’t want it to fall to bits. Brian pulled the boot off to find that the impact had broken the circlip that retains the shaft in the CV joint. He had a spare in one of his many drawers of bits so that wasn’t a big problem. I just need to clean it up and make sure I recover the fragment of circlip before greasing it up and reassembling it. The outer CV joint didn’t feel too good though and needs replacing, so I’ll get one ordered on Tuesday. Brian stuck the shaft in the lathe to check that was still straight which it fortunately was.

Very little got done on Sunday due to golf (yes, I made my comeback!) and work in the evening. I did manage to degrease the front and rear subframes and make a start painting them. I was working again on Bank holiday Monday morning but managed an hour or so in the garage beforehand and got the subframes completed. In the afternoon I got the wishbones and remaining suspension bolts painted. The wishbones just fitted in the oven so they were easy enough to cure but the subframes were a bit too big. I had a cunning plan involving using my heat gun to heat them up enough to cure the paint but it didn’t really get them hot enough. Curing it isn’t essential but increases its resilience. I have a feeling they might fit under the lid of my gas barbecue though …

So, it feels like I didn’t get all that much done over the weekend but I’ve got lots of parts that are now ready to bolt back onto the car and I fully expect progress to be fairly rapid now. The Jury’s out on whether the car will be ready in time to make it to Oulton Park on the 10th September, it’s not impossible but it’s going to need a huge effort. I’m quite good at huge efforts though :)

The rebuild commences

With the repaired chassis back in the garage it was time to start thinking about where to start. The arthroscopy went fine and in fact I was in less pain post-op than I expected and was back in work the day after. Kneeling and bending are out though and getting around the obstacle course that the garage has become with a whole car’s worth of bits strewn all over it was a bit of an issue. Here’s a shot of the main dash cross rail, Brian’s grafted in a short section in the middle, internally sleeved to beef it up a bit.

I’d made a start on painting the bolts – I came up with the idea of making them into little garlands using some lockwire. They could then be hung up and sprayed using the airbrush. This worked nicely but there are a lot of bolts …

Another thing Brian had noticed was that the fuel tank had slid across slightly. This was hardly surprising really but meant the tank covers had to be removed to loosen off the central strap. I also used the opportunity to paint the threaded rods that retain it at each side as these were also bare metal and had assumed the dreaded reddish tinge. Here’s the repaired front corner of the chassis.

I cut out a triangle to replace the damaged part of the nearside side panel using the new side panel as a template. This made it easy reusing all the same rivet holes. Once that was done I could start prepping the chassis for some paint. The floor panels got masked off along with the rear end of the chassis. For the etch primer I had a go using the airbrush again, this meant it took a bit longer but gave me much better control of where the paint went and reduced the amount of the stuff landing where I didn’t want it.

Once that had hardened it was time for some of the high build primer, I did consider just going straight ahead with the top coat but decided this stuff would help blend in where I’m going from the previous paint to bare metal. I used my normal spray gun for this although I stuck to the touch up gun rather than the big one, apart from the control it just seems to give a better spray.

One problem emerged after this – the VIN was getting filled in even though I was pretty careful with the high build primer. So I attacked it with the wire brush in the drill and masked it. I’ll stick some clear lacquer over it later.

Once I’d done a bit more work masking it was ready to turn the garage green again :-) This went pretty well and while it was drying I swapped the compressor hose to the shed and sprayed the etch primer on the new side panel.

 

Each prang in a Fury usually results in needing a replacement steering rack, usually along with fixing the rack mounts. Because the steering rack in the BDN is mounted behind the bulkhead it’s pretty immune from the impact although one of the threaded end pieces is a bit bent. The rack is a bespoke one produced by Titan, so I rang them to get a new part. It’s basically a 1.5″ long 7/16″ UNF threaded bar with a little ball on the end. £32.99 plus VAT and delivery was a bit of a shock to be honest and seems completely extortionate but having had a chat with Brian straightening the old one isn’t really an option so I gritted my teeth and rang them back and ordered it. And here it is, doesn’t really look a lot for 40 quid, does it?

I’d taken Monday morning off work after my op but was back in Monday afternoon.By Thursday the swelling had pretty much gone, I was back in the gym and walking without a limp. It wasn’t really impeding progress with the rebuild. However I didn’t get back out to the car until Saturday morning. I got the remainder of the bolts painted and got the front bulkhead refitted. I spent an hour or so in the kitchen giving the bulkhead a bit of TLC the other morning so it’s looking a lot better. I could then put the bends in the offside side panel and the nearside triangular section and drill the rivet holes in the new tubes.

I lost quite a bit of the morning replacing the brake pads in David’s Civic – took a bit longer than it would with the Wilwoods! Once the bolts were dry they went in the oven for 10 minutes at 175°. Like doing a pizza but smells much worse! I got the fuel tank refitted and replaced the covers. The side panels then went up to the shed and got a coat of black paint on their inside surfaces.

On Sunday morning I cleaned the paint off the engine stays – they were originally painted with an aerosol rather than 2 pack from the gun and it just isn’t as hard so they were looking decidedly tatty. 10 minutes with the blow lamp and wire brush followed by a clean off with some thinners and they were ready for a coat of the black self-phosphating paint. Before painting them I’d checked that the longer one fitted in the oven which it does, just.

While they were drying I could get the side panels riveted on. I then gave the rear bulkhead a clean up and refitted that and torqued up the bolts. The engine stays got baked n the oven to cure the paint and look much better than they did before. I then just about had time to bolt the pedal box assembly back on before heading off to work on Sunday evening.

Back to meet its maker

The chassis went back up to Hereford on Monday evening. I hadn’t seen the chassis jig before but in true Baldwin style it’s very impressive! It’s made of 4″ x 2″ steel box section and like all things BDN was designed by Ian and fabricated by Brian. It’s on big castors but once in position the threaded feet were lowered and adjusted to make sure it was square. It has lots of machined pads on it with lugs to locate the chassis tubes, these were removed as the chassis still has the undertray on it. It has a separate structure at each end with a machined aluminium plate to match the bulkheads to which the water jet cut end plates are bolted prior to fabrication of the chassis.

We got the chassis up on the jig and that was that really. Brian will bolt it all up to make sure it’s straight then will cut out the damaged tubes and replace them. He’s also going to check over the rear subframe and the engine mounts. The plating on my subframes and wishbones was a bit of a disappointment – I think it deteriorated when I took the car for its exhaust in Cardiff when there was salt on the road. Brian and Ian have a new approach, initially stimulated by the requirements for Ian’s brother Rob’s car which he’ll be racing in Australia where race car suspension parts aren’t allowed to be plated. So they’ve found a self-phosphating paint for all these parts and are using it to dip the bolts etc. as well. So once it’s back together my car really should look better than before.

I ordered replacement brake disk, cunifer brake pipe and a couple of other bits and bobs from Rally Design. I also made a trip to our local paint emporium for a load of stuff – more etch primer, high build primer, satin black as well as both white and green two pack.

My gearing’s been all to pot, always over-geared. My original calculations were based on a slightly wrong wheel circumference that I’d got from somewhere and even at Snetterton I wasn’t needing to use 6th gear at all. One thought was simply that I just wasn’t going fast enough but watching everyone else’s videos my maximum speed of 126mph was within a couple of mph of Austen and Tim so I actually wasn’t doing too bad there. I then recalculated my gearing based on my logs, i.e. I looked at the relationship between rpm and speed in 5th gear to calculate back. This turned out to be interesting as I ended up with inconsistent numbers! I guess this is due to the tyre circumference actually changing slightly at speed and possibly very minor degrees of clutch slip. I’m currently running a 50 tooth rear sprocket and decided to go for a 51, 52 and a 53 so I got those ordered from Talon Engineering, I still opted for their optional lightening holes but didn’t bother to pay to have them split this time as they’d clearly done nothing cleverer with the previous ones than cutting them in half with a hacksaw and I can do that. I also ordered a new chain from my friend Richard at M&P.

Another thing I did was bite the bullet and shell out for some video overlay software. Tim Hoverd uses Trackvision to good effect but when I’d had a go I couldn’t persuade it to import the data from my DigiDash. I’d also had a play with some software called TSX Overdrive with the same outcome. So I downloaded both of their demo versions and had another go. It ended up not being much of a decision in the end as TSX simply wouldn’t run on my Windows 7 laptop at all! After half an hour or so I had Trackvision happily importing my logger data and I found I was quite easily able to edit the text based dash configuration files to show what I wanted to I bought the full version of that. After a bit of fiddling here’s where I’d got with my custom dash. What’s interesting is that it’s massively more instructive in terms of analysing my driving than using the log analysis software particularly using the brake indicator to look at braking points and the G circle to look at cornering. This is a single lap from the testing on Friday, I did go slightly faster in the last session but the camera lens was covered in crap. The sound’s rubbish but that’s because of a camera problem at the time.

On Friday I made a start on tarting up all my fasteners. The bolts that retain the bulkheads and subframes along with all the suspension bolts are 12.9 grade high tensile and come in what I think’s called ‘self colour’. It means they’re a sort of black to start with that goes red when it’s been in my garage for any length of time! I did have a cunning plan to replace them all with zinc plated ones to look better but Ian wasn’t terribly happy as he says the plating affects the strength of the bolt. I gather it’s something to do with hydrogen embrittlement – yes, I did look it up on the web and no Ian, it’s not because I didn’t believe you ;) So I got them all together and cleaned them up using a wire brush mounted in the lathe then soaked them in petrol to get all the oil and grease off them. I’m doing to do what Brian’s done on Rob’s car which is to use the self-phosphating paint. One option is to dip them which means making up some form of rack so you can dip each end, they then need baking in the oven for a while. I decided I’m going to try spraying them and on my little shopping trip to Machine Mart on Friday I got a cheap air brush which should do the trick.

I’ve kept in touch with Brian during the week and he’s been fairly happy with his progress on the chassis. He’d been hopeful all along of having it ready this weekend and when I spoke to him on Friday evening he was sounding pretty pleased with himself and was confident it would be ready Saturday afternoon. So I plan to get it back later today after my weekly drubbing by David at the golf course – I have little chance these days, last weekend he played 6 shots better than his 9 handicap despite taking 7 on a par 3. I’m not sure at the moment when the BDN rebuild will resume, or indeed when I’ll be golfing again as I’m having the torn cartilage in my knee removed tomorrow. It’s being done via an arthroscopy and I’m hoping to be mobile again pretty quickly but you never really know.

More stripping

While I was waiting for Brian and Ian on Saturday morning I made a start on stripping the bearings out of the mangled wishbones. There’s a combination of rod ends, spherical bearings and acetal bushes. The spherical bearings are held in with a circlip one each side so after removing the circlip each bearing could be pressed out using the tool I made to put them in in the first place. The bearings all seem fine although a couple of the housings were a bit deformed. The trouble is they feel OK when loose in your hand but it’s difficult to check them for play etc. so I’ll check them all carefully once they’re installed in the new wishbones.

Once the Baldwins arrived we pulled the trailer out into the sunshine so they could have a good look at the chassis. We removed the front machined bulkhead which had had a slight curvature to it, Ian had said he’d be surprised if it wasn’t OK and indeed as soon as it was unbolted from the chassis with no stress on it it was straight. It’s a hard grade of aluminium alloy with some copper in it apparently and it certainly seems to be up to the job. After some measuring the conclusion was that apart from the obvious damage the rest of the chassis was OK with no twist in it. Brian also reckoned he could replace the tubes OK without removing the main undertray/floor. He wanted to get the chassis back oto the jig he’d used to fabricate it in the first place though and that meant I needed to remove the rear subframe, the rear bulkhead and of course the engine …

Brian and Ian left at lunchtime so after some lunch I get the spanners out and got going stripping the rest of the stuff off the car. First of all I removed the right rear suspension, then the body mounting frame and rear undertray followed by the rear subframe (which seems unscathed but Brian will also check it against the jig he made that on). I made surprisingly light work of getting the engine out and had it done by just after 3pm.

The engine bay was surprisingly messy with a combination of soil from the off, loads of bits of rubber and a general film of dirty oil. I decided I might as well go for it so I removed the battery, master solenoid, catch tank and then the loom came out as well. This allowed good access to clean it all up.

The whole underdash panel came out with the loom then I removed the fire extinguisher hose and this is what the front end looked like then. All I need to do now is remove the rest of the offside side panel and the lower triangle of the nearside one then the chassis’s ready to go to Brian, hopefully on Monday evening.

No rest for the wicked

Not that I actually think I’ve been wicked really. Anyway, having discarded the option of throwing in the towel I decided I’d better fix the car. So after my long drive home on Sunday I pushed the trailer with the car still on it into the garage and unpacked all the tools from the motorhome. And I made a start on it. all the bodywork came off, some of it rather easily as it wasn’t actually attached any more. I then removed the offside radiator ducting, drained the radiator and removed that. I unbolted the completely wrecked aluminium bonnet mount frame and removed the throttle cable and master switch wiring from down the side of the chassis.

I’d already had a chat with Brian on Saturday afternoon but had a longer chat on the phone on Sunday evening. I’d also emailed him some photos and he’d had a chance to see the video. He was already on the case of working out what parts were likely to be needed and was as usual very helpful and pragmatic.

My leg was a bit sore but I managed to get to the gym on Monday. My head was mostly in the shed all day though. I spoke to the VOSA inspector who again was very friendly and helpful and simply said to give him a ring when I’m ready although he warned me he’s away the first two weeks of September. I also rang Rimstock to order a new set of wheels but couldn’t get hold of the guy who deals with motorsport wheels. In the evening I got to work dismantling the car a bit more, removing the front upright assemblies followed by the mangled wisbhones and broken steering arms and suspension pullrods. The wishbones have of course been very carefully designed to only be as strong as they need to be to avoid the situation where the wishbone stays intact but takes out half the chassis as it did on my Fury. What’s impressive is that although all four of the front wishbones are very seriously damaged with the upper ones having complete Z bends in them all the welds are fully intact.

With the suspension removed I then got the undertrays off and then removed the front subframe. This doesn’t appear to be too badly damaged and it may be that Brian can re-jig it and replace one or two of the tubes rather than making a whole new one. I then dismantled the ARB, the suspension bellcranks and dampers. I then removed the pedal assembly and the GRP moulding containing the hydraulic fluid reservoir followed by the steering column and steering rack. I drilled out some rivets and peeled back the side panel so I could have a better look at the lower chassis rails. These do indeed have a slight bow in them which is a pity as it has significant implications for the amount of dismantling I need to do. I removed the clutch and rear brake lines as they were damaged anyway and will need replacing.

When I came in I had another chat with Brian updating him on what I’d found as I further disassembled the car. He’s remaining hopeful that we might be able to fix the chassis without removing the floor panel which would save a lot of work. There’s even a possibility of being able to leave the engine in, the plan currently is for me to do a bit more dismantling then he’ll come over and check it over and do some measuring and work out the best way forward.

By now the garage was a bit of a tip with tools and parts everywhere. The bodywork takes up quite a lot of space so I took the hardware off the front cover and stuck it outside, it’s scrap anyway. I sorted out all the bits, tidied up the tools and cleaned up all the bits of grass, soil etc. from in the car and the brake fluid that had leaked when I disconnected everything.

I got hold of Mark Wain in Rimstock on Tuesday and ordered some wheels. Sadly they’re about to shut down for 2 weeks so he reckoned it will be 4 weeks before I’ll have them so that may well be my rate limiting factor. And of course then the IVA inspector’s away for a fortnight.

Tuesday evening my mate Phil came round to give me a hand. He’s very handy with the spanners and it’s nice to have a bit of company in the garage. I had been planning on completely dismantling the dash and its wiring but Brian thought it would be fine if the aluminium base was just removed and swung out of the way so that’s what we did. The top end of the steering column and gear cable mount came off. The nearside sidepod and rad ducting came off – one saving grace has been that both radiators are unscathed.

We then turned our attention to the rear. When the rear of the car slapped round into the armco the impact on the rear wheel broke the nearside brake disk and the upright. It also pushed the diff across a little. So with the wheel off we removed the hub nut, unbolted the wishbones from the upright and took off the upright. The driveshaft was fairly easily persuaded to come out of the diff. We then removed the offside upright and driveshaft – the wishbones etc. on the offside are intact. The impact had pushed the diff through the nearside bearing carrier so it looked like this was undamaged but the carrier mounts on the offside are clearly bent. The offside wishbones and upright were undamaged but the wheels pretty damaged presumably from its interaction with the pit wall – unfortunately I slid along it and hit the beginning of the armco which I think sticks out a bit from the wall. By then it was 10pm and time to call it a night.

On Wednesday I got a bit more done in the morning then Phil came round again in the evening and we stripped the rest of the rear end – we unbolted the diff carrier and checked that for damage. It all seems OK, I removed then refitted the nearside bearing carrier. It looks like the clevis and adjuster on the enarside are fine but the offside one is a bit second hand as is the pair of aluminium block which act as a mount for both the lower diff carrier and the damper – as well as the bolt being bent the pair of aluminium blocks have got a bit deformed.

We removed the rear cockpit bulkheads and I removed the remaining fittings from the dash rail then that was about it until Brian comes to have a look at it. I then gave Brian a call and it looks like he and Ian will be coming down on Saturday to have a look at the best way forward. I know Brian could do without all this extra hassle when he’s got his work cut out building Rob’s car but he’s been incredibly supportive, working out what parts we’ll need. He’s already sorted out the replacement wishbones – he tacked a set together and took them over to Bob at Concept Racing on Monday and collected them yesterday! With Ian to advise on which bits are structurally OK to straighten/reuse (after all materials engineering is his day job and he’s’ done all the calculations on the components) and Brian actually doing the fabrication I’m supremely confident the chassis will be as good as new.

We’ve talked about whether anything can be done to strengthen that part of the chassis to prevent cockpit intrusion and the problem is there isn’t much room as you need to be able to turn the front wheels. The AB Performance Sabre has a structure of tubes a bit like radial spokes with the hub centre a little way outside the chassis to make it a bit more 3D but in reality I suspect that when you have a big impact and the edge of a wheel hits the tubes they’ll just fold anyway. At the end of the day whatever you do is a compromise and if you try to engineer for every possible collision you end up with a car which is either overweight or unaffordable. The bottom line is that despite a pair of very heavy impacts I was still able to spring gazelle like from the car! That bit of the video seems to have impressed people :)

 

So here are a couple of shots of the car as it is presently. It’s looking a bit sorry for itself but once the chassis is sorted I’ll soon get it back together.

 

The garage is in a bit of a state too. I think while I’m waiting for the weekend I’ll sort out all the bits of GRP. At the time of the crash I made quite an effort to collect all the little bits since it’s best to make a decision later in the cold light of day about what’s repairable and what isn’t. My current thinking is that both sidepods are repairable but both need new floors. The front cover is toast but the rear cover is not in a bad state and will be fairly easily repairable.

“Motorsport is dangerous”

Most readers of the blog will probably already be aware that I had a big shunt at Snetterton on Saturday. A chaotic start mainly due to Tim H stalling led to Colin pushing me into the pit wall. I survived this and carried on although I suspect there was quite a lot of cosmetic damage by that stage. I’ll never really know how much however as exiting the second corner complex at Montreal Sam Cook in Tim’s old Fury dropped a wheel off the kerb and spun, coming back onto the track right in front of me. I couldn’t avoid him and hit him pretty hard with my right front corner. This smacked my wheel into the chassis taking the throttle cable with it so I had no steering and was at full throttle spearing off across the grass to the armco on the left. As I bounced across the grass I was trying to reach the kill switch and think I managed it just before hitting the armco. This was another big impact and caused extensive damage to the left hand side of the car.

I got out of the car pronto and jumped over the barrier and reassured the approaching marshal that I was OK. My right leg was hurting but I knew it wasn’t serious. We were shortly joined by lots more marshals and the medical car followed by the recovery trucks. Sam was pretty shaken and had a sore neck, he was profusely apologetic but it was a racing incident and there was nothing to be gained by bad feeling. Colin was in the medical car as they’d picked him up off the grid then immediately got the call to come to our crash. He thought someone had tagged him at the start pushing him over into me. He wasn’t hurt. One of the recovery trucks was driven by Ian Baldwin who was of course pretty gutted seeing one of his babies embedded in the armco. Ian took lots of photos of the scene and we collected all the debris up and got the car onto the recovery truck.

Here’s the footage from my car followed by the view from Tim’s car.

To say it’s disappointing would be an understatement. During the test sessions on Friday the car had felt dramatically better than at Donington and I’d steadily improved on my fastest lap of 1:26.2 from the last visit to Snetterton in May with 1:25.8 in the first session, 1:24.8 in the second, 1:23.96 in the third and 1:23.8 in the last session by which time I was getting knackered. The car had been fine apart from a minor gear shift issue in the morning due to the gear lever’s pinch bolt falling out. I was still well off the pace of the folks I was racing against in the Fury towards the end of last season but I was improving and getting more confidence in the car.

The car’s pretty badly damaged, the only corner not damaged much is the right rear but even that wheel’s trashed from scraping against the pit wall and the beginning of the armco after it. Chassis damage seems to be limited to the front right corner and although it will mean completely stripping the car fixing the chassis shouldn’t prove too difficult a job for Brian.

I suffered some bruising to my right lower leg where the chassis rail got bent in and the inside of my right knee presumably from the steering column but apart from that I’m physically fine. Neck and shoulders were fine. I was wearing a HANS but I’m reluctant to attribute much to this, I was also fine after a nearly identical shunt at the same corner 2 seasons ago and after going head on into the barriers at Mallory when the Fury throttle jammed open.

The RGB paddock’s a great community and I was very grateful for the support of my many friends during the evening. By the end of the evening my leg was hurting quite a lot so I retired early and headed off home on Sunday morning. As the Governor of California once said, “I’ll be back” …