Monthly Archives: September 2011

Oulton Park

After a 22 hour session in the garage, an hour and a half’s sleep and a 4 hour drive we arrived at Oulton at 10am. Brian and Colin set about getting the car off the trailer while I went over to register and sign on. The RGB guys were already in scrutineering but qualy wasn’t till 11.25 so I wasn’t too pressed for time. Once signed on we tightened up a couple of bolts I’d remembered and tightened all the suspension pullrod nuts – the car ride height and corner weights hadn’t been done but there wasn’t enough time for that.

I took the car round to a deserted scrutineering bay and was there all of 3 minutes while the scrute did a very quick check over the car. He went off for the ticket and came back asking my name as I wasn’t on the list. I just said I was a late entry, I thought if I told him we only finished rebuilding it a few hours ago he might have wanted another look!

I now had to try to get my head together to actually drive the car. Despite the fact that my last few moments driving her had been pretty horrific I didn’t really have any “getting back on the horse” feelings but it’s always an odd feeling going out on a race track in a car you’ve just put together yourself! I got noise checked and drove into the assembly area to receive a quite amazing welcome from the RGB crowd, applause as I drove in and lots of handshakes etc. What an amazing feeling.

It was a pretty depleted crew, my entry took the numbers up to just 13. I was glad to be at the back, this was never going to be anything more than a shakedown session. We were on the Fosters Circuit, a configuration I hadn’t driven before, so as we swooped down Cascades instead of turning left and going along the lake to the Island hairpin we had a little kink left then a sharp right. The car felt fine, brakes were fine and the lower gearing was quite noticeable. I took it very steady round the lap then as I came around Cascades again the engine cut out. A glance at the dash told me the electrics had gone off completely. I pulled off onto a service road and behind the barriers and got out. It had to be something in the master switch circuit, so I lifted the bonnet and bypassed the external button and the dash lit up again. So I got back in, belted up and headed off out again. I managed another lap before it did it again almost in the same place so I pulled off onto the grass in the infield. I tried switching off and on a couple of times and it came back to life again, so I went back out.

It cut out again a couple more times but each time a few presses of the button and it came back on again. I wanted to make sure I strung together enough laps to get me on the grid.
Another problem was that my speedo wasn’t working – the wire from the sensor had looked a bit suspect but I’d hoped it was OK. Clearly it wasn’t! This meant that as well as no speed indication I had no gear indicator.

We now had well over 4 hours before the race so there was plenty of time. I was keen to blame the master switch toggle button but Brian wasn’t – he reckoned they were pretty good quality and unlikely to fail. So we had a look at all the connectors and eventually Brian discovered a dodgy one in the engine bay, when he wiggled it he circuit broke. It was a bullet connector that looked like it just hadn’t been pushed together tightly enough. So we thought that was that problem solved.

We took the car round to the scrutineering bay with the corner weight scales and checked that over. The ride heights were a bit out but once we’d sorted those the corner weights were very close so we didn’t bother with too much fiddling.

I managed to catch 40 minutes snooze in the afternoon. I swapped the harnesses – the original ones were 3” belts and didn’t work particularly well with the HANS, so I’d got a set of Schroth harnesses designed for the job, 3” harnesses but with 2” shoulder straps.

My lap times were unsurprisingly abysmal and I was 13th on the grid although the actual grid box is labelled 12a! I knew that with my lower gearing the chances were that I’d get an even better start than usual but my game plan was to make sure I was 13th going into the first corner! And indeed the second corner. Lee Baverstock proved the fly in the ointment as he had an appalling start and he was behind me going into Old Hall so I backed off till he’d gone through. I sat behind Robert Gardiner in his Fulcrum for a lap or so until I’d gained a bit of confidence then got past him on the brakes down the hill from Cascades. Next in front was David Lawrence in his Riot and I got past him without too much difficulty. David Masters in his red Fury was the next car but he was quite a way in front. I did start to make inroads into the gap but my coolant temperature alarm came on. This was offputting enough to slow me down a bit but then the electrics cut again. Robert came past me by the time I hit the button a couple of times and got it going again. Not long after that my oil temperature alarm went off as well so I limped round till the chequered flag.

Sadly no video as I simply didn’t have time to refit it and forgot to take it with me to Oulton.

So, a couple of things to sort out. The cooling seemed to me to be pretty certain to be an airlock in the system – I simply hadn’t had time to run the engine up to temperature before heading up to Oulton Park. The speedo is a quick fix with a new sensor. The electrical problem is a bit of a bugger though. Brian suggested I have a look at my logs to see if I’m getting a volt drop which might then trip out the electronic battery isolator. Top culprits are either the isolator itself or the battery. There’s also a problem with the reverse so I think that puts the battery in pole position.

To say I was a bit knackered after driving the 215 miles back from Oulton would be a bit of an understatement! I stuck the car into the garage still on the trailer and left everything in the motorhome and hit the sack. No time to sort any of it out next morning as Jen and I had to leave the house at 10am to fly for a week in Majorca – I hadn’t even started packing!

After a week chilling out in Majorca I came back and unpacked everything. The garage was in a real mess! Once I’d tidied up and got the car off the trailer I made a start on looking at the cooling system. I refilled the system and ran it up to temperature at which point I spotted water coming from under the car. I though it was coming from the nearside sidepod and feared that the radiator was damaged. After stripping the sidepod and ducts off all seemed OK there and I eventually tracked the leak down to the water pump housing. This puzzled me until I stripped it to bits and discovered that the chain had paid it a brief visit when it got derailed in the crash at Snetterton. It had caused a small split in the hose and a dent in the inlet spigot to the pump. The fix was quite easy, just replacing the whole water pump with the one from the stricken engine sitting in the garage. I then refilled the system and ran it up till the fan came on and confirmed there were no leaks.

Next puzzle was the electrical problem. Firstly it’s cutting out occasionally but second the reverse has never worked properly – instead of pulling smoothly it chatters and drops the volts enough to reboot the DigiDash. The likely culprits were either the battery or the electronic isolator master relay. My first experiment was to check the logs which confirmed that right up to the split second the electrics cut it was running around 14 volts. Next I removed the relay from the equation by disconnecting the battery cables form it and bolting them together thus bypassing it completely. And hey presto the reverse worked fine with no chatter. The trouble is this doesn’t actually definitely pin it on the relay, Brian’s concern was that I’m using a smaller battery than theirs, a problem compounded by it having very small terminals and he was worried that there’s a risk the reverse is dropping the voltage enough to unlatch the master relay. This still doesn’t explain the cutoff during the race though. When taking the battery out I did discover that the positive terminal screw wasn’t tight which could be an explanation.

So, I’ve ordered a new battery (a Red Top 20 instead of the existing Red top 8) which has much beefier terminals in addition to a higher capacity. I’ve also ordered a plain old cutoff switch and a cable so that if the new battery doesn’t solve the problem I can convert to using a plain mechanical cutoff switch and a pull cable. I’ll book testing on the Friday at Pembrey next weekend so should have plenty of time to sort it if there are still problems.

So, a bit of work to do during the week but nothing like the same pressure as the week leading up to Oulton!

Final push

Well it was a really early start on Friday, I was out in the garage by about 5am. Sitting here looking back on it on Sunday morning it’s difficult to remember what we actually did and in what sequence because there was so much of it and it’s all become a bit of a blur!

My first job of the day was to make a start on the new front splitter. I’d bought a sheet of B&Q’s finest 6mm marine ply on Thursday and although the old was was destroyed there was a large enough piece to allow me to use it as a template. I got that marked up along with the 2 strips of 12mm ply used as spacers and once we reckoned it was OK to start making a bit of noise I got them cut out and sanded. Andy was prepping the body panels so I took the splitter parts and the front rad ducts up to the shed and sprayed them black.

While Andy completed prepping the body panels for there topcoat I got on with the mechanical stuff. I got all the wiring in the engine bay connected up, fitted the rear radiator ducts and the oil cooler then filled the cooling system. I then had the engine running again by about noon.

The dash panel got screwed back on and the wiring for the lights etc. laid out. I refitted the rear undertrays and the rear bodywork mounting frame then the exhaust. Then round to the front to fit the splitter. Andy had all the bodywork painted soon after lunch and he then made a start on the headlight pods, cutting out for the lights and fitting rivnuts. I got the front radiator ducts fitted but couldn’t finalise that till the bonnet was fitted.

Eventually it was time to get the wheels on and lower the car back down onto them. We set up the aluminium angles and string lines and set up the geometry – of course on the BDN the camber is fixed so this was actually quite quick once we’d got the string box set up, just a matter of adjusting the steering rods at the front and the track control rod at the rear.

Once the bodywork was dry and we could handle it we made a start on fitting that. We fitted the bonnet first and sorted out the position of the front radiator ducts and got them screwed onto the side panels. We then bonded in the nearside light pod base and stuck some bits of wood underneath to support it.

We’d had to dismantle all the lighting from the rear valance so once that was dry Andy refitted all the lights to it and I rewired them all. The other headlight pod got bonded in and wedged in place. Once that was dry enough to move we could make a start on fitting the sidepods. These still needed some trimming to clear the front rad ducts.

Once they were fitted we could refit the rear bodywork and the rear valance. Andy fitted the new front light units and we got them connected up and tested. This all sounds pretty easy but it took a lot of time. Quite a few things had to be redone as we were making mistakes under pressure and through tiredness, it got progressively more difficult to find stuff as the garage got more and more cluttered – with so many jobs on the go and so little time you simply can’t put things away when you’ve used them. Midnight came and went and we still had loads to do, lots of fiddly stuff. Fitting the body catches on the bonnet took quite a time. Tidying up all the wiring, fitting rain light, the dash sub panels and DigiDash, refitting the bulkhead panels, headlight covers. I slapped some race numbers on and we declared her ready to rock and roll.

It was 2.40am. We were both shattered. Scrutineering was at 10am 215 miles away. I got into bed at 3am and of course couldn’t get to sleep. The alarm went off at 4.30, I got up, juggled all the vehicles round, we got the car onto the trailer and rounded up some tools and loaded them into the motorhome and headed off at 5.50.

So we did make Oulton Park, I had a few issues but the car drove great and came home in one piece. I’ll write up a bit more later but I have a plane to catch.

A massive thanks to my brother Andy who worked like a trojan to get the car there. Also to Brian who got the chassis and all the other bits and pieces sorted quickly and has been a great support.

Down to the wire

On Saturday morning I got the ARB push/pull rods fitted and the steering rods bolted onto the uprights. I also fitted the reverse motor and completed the assembly of the engine mount plates. Brian has modified my starter by cutting off the end of the shaft and the ‘nose’ of the pinion so it finishes flush at the end of the pinion.

Andy then got up (lightweight ;) ) and we got going on the sidepods. These require quite a bit of work trimming all the edges and they’re very 3D so difficult to get your head round them initially. Once I’d made a start Andy did the marking and I did the cutting. While Andy sanded the edges of the sidepods I got their floors ready and David helped out sanding the edges of these, they require quite a lot of work particularly along the outside edge where the strip of ply is embedded in the moulding.

Once one set was ready I got on with bonding the sidepod onto its floor using PU sealant and some pop rivets, by this time the second one was ready to assemble. While I was doing that Andy bolted the clutch slave on and got that connected up then made a start on bleeding the hydraulics. Once I’d finished the sidepod we finished off bleeding the brake system.

After lunch we set about the sidepods, getting them held up to the car and trimming to go around the roll cage, brake lines etc. Once these were done we made a start on the front cover. This needs a lot of trimming so it sits nicely on the dash cross rail and fits around the front of the roll cage tubes. This took quite a time and by the time it was ready to bond onto its hinges my time was up and I had to get ready for work.

Lots of time on Sunday was spent prepping bodywork for paint. We bonded the bonnet onto its hinges and while that was going off we got going on fixing up the rear bodywork. There was a chunk missing from the front of the the engine cover, quite a bit of damage at the rear corner and cracks in both wheel arches and the rear valance was damaged in a few places. We got them cleaned up, superglued the cracks (Andy’s done this before) then got going with the fibreglass mat and resin. I also waxed up the old sidepod and started to make a plug to replicate the fuel filler recess.

Once the bonnet hinges were set we bonded the sidepods onto their brackets and carried on repairing the other bits. When we were confident the sidepod adhesive was set we took the bonnet off and got that prepped for paint. We had to cut out the headlight apertures, trim the air intakes and trim all the returns. We then got the sidepods off and prepped those. It was well into the afternoon by the time the first sidepod was ready for paint so I was starting to feel rather more pessimistic. Andy did the spraying while I carried on with the other bits and pieces. Sadly he ran into the same problem as me with contamination along the mould lines causing problems with the paint. You try sticking more paint on but it makes it worse :(

With a sidepod done Andy painted the bonnet, again with problems and quite a bit of it needs rubbing down and doing again. By 4pm Andy had to head back home. With me working away Monday to Wednesday things were looking a bit bleak – there was still loads of paint to be done and some of the bodywork wasn’t even ready for paint yet. There was also still quite a bit of minor mechanical stuff to do. Andy had somehow become infected with the motivation to get the car out for Oulton Park though and after a brief negotiation with his wife decided he’d come back down on Wednesday to help out.

Once he’d gone I put some time in sorting out the fuel filler plug then sanded and cleaned up the rear valance and took that up to the shed and gave it a coat of filler primer. After a quick tidy (the garage was looking like a small thermonuclear device had gone off in there!) I called it a day and went in to get some of my prep work for this week’s trip. I did of course take a break to watch Dragon’s Den in which our sponsor Andy Bates made his pitch to the Dragons and came away with a cash investment and a tall business partner in the form of Peter Jones. It was a very impressive performance, Andy was superbly well prepared (and in a suit!!!) and did himself proud. I suspect he got exactly the result he’d hoped for.

On Monday morning I just had time to slap some polyester resin and chopped strand mat on the fuel filler plug but that was about it. I was off to Swindon then for 3 days. Andy arrived Wednesday evening so Thursday morning we made an early start. I bonded the new filler neck moulding onto the sidepod before heading off to work while Andy got going stripping the dodgy paint off the front bodywork. I had a bit of a day from hell in work but got home to find Andy had got all the bodywork primed. We didn’t have time to get much done in the evening but did get the mesh screen bonded into the front radiator ducts. The wheels had arrived from Rimstock on Wednesday and my younger son Chris had taken them down to our local ATS and got the tyres fitted so that was one potential show stopper out of the way. Colin had also been in touch with Chris Norman, race secretary at the 750 Motor Club, and he’d taken pity on me and sent me a pair of Oulton tickets so I could get into the circuit if we do make it.

So, it’s a mega early start today with a lot to get done. If we don’t have any significant hitches there’s a good chance I’ll be at Oulton Park tomorrow.

The spanners fly

After a rather frustrating weekend I was keen to get on with actually bolting more bits back onto the car. I did a bit more ordering on Tuesday – a replacement CV joint (cheaper to get one delivered from Ebay than buying locally) and a new harness. I suspect the old harness would probably be OK but I decided to replace it partly to play safe but partly also cos the old one had 3″ wide shoulder straps which don’t work terribly well with the HANS.

Tuesday evening I fired up the barbecue and cooked the subframes – glad Ken Greenway wasn’t around or they would have ended up smothered in Reggae Reggae sauce ;) While they were chargrilling I did a bit more refitting of parts – the battery, ECU. It was then time to start on the electrics. I’d removed everything in one go – dash, loom, master solenoid etc. so it all went back in one go. As these things usually do it took longer than I expected as the routing’s quite complex around the engine bay so I didn’t get much else done.

On Wednesday evening I refitted the diff mounts, rear damper mounts and bellcranks onto the rear bulkhead. The painted bolts really do look much better although they now make some of the plated flange nuts look a bit scruffy. I then fitted the new offside diff carrier (the old one had got a bit bent) and got the diff refitted. The rear subframe went on next which involved removing the battery and master solenoid I’d fitted the evening before :( I then cut my shiny new 53 tooth sprocket in half and got that fitted – interestingly after telling me on the phone the sprockets would be 2-4 weeks I received them from Talon Engineering after 3 working days! And here’s the new look black subframe making its first appearance on the blog. The finish is pretty durable but of course it will get dinged by spanners and stone chips, as indeed either nickel plating or powder coating would but at least I can touch this stuff up.

The CV joints arrived on Wednesday – much easier mail ordering than buying locally! Saved me about an hour of time and a couple of quid of diesel. Thursday morning saw a bit more ordering – more of the nasty adhesive from RS Components and I ordered some new flange nuts too. Also some replacement bolts for the sprocket – the trouble with buttonhead socket bolts is that as soon as you apply the kind of torque required the socket deforms.

Brian had got the front bodywork laid up early in the week but collecting it was going to be a bit of a problem. It won’t fit into the Audi, my mate with a Transit is going off to do the Woodpecker rally in Leominster and I’ve conceded that Brian’s probably right that trying to bring it back on the trailer is a recipe for disaster. Phil is available with his Transit on Sunday but that really leaves me with little chance of getting the bodywork fitted/painted etc. in time. So I thought of hiring a Transit. Then remembered that I’ve got one on the drive. Doh! OK, so it’s masquerading as a motorhome but it’s pretty big and getting the front cover through the door shouldn’t pose too much of a problem.

On Thursday evening my Brother Andy arrived for a couple of days. He thought he was coming for a couple of days break but I soon disinvested him of that ridiculous notion and ushered him into the garage :) We got all the spherical joints pressed into the wishbones and the retaining circlips fitted, along with the nylon top hats and the centre bushes. He was then allowed a beer.

Friday morning saw an early start. We got the nearside drive shaft sorted – replaced the outer CV joint for a new one, cleaned out then repacked and refitted the inner one and replaced the boots and put new clips on. We then got going sticking the rear corners together. I reassembled the nearside upright, we fitted the drive shafts then the wishbones followed by the uprights. We hit a slight snag when we found the whole lot was binding and wouldn’t turn. After some head scratching and disassembling we discovered the new disk on the nearside was the wrong size, I’d ordered a 10.5″ instead of a 10.25″. Doh! I rang Rally Design and ordered a new one which is due to arrive Monday – Saturday delivery was another £19 so I decided to wait.

We made a start on fitting the front suspension mounts to the bulkhead but took a break late morning to go up to Hereford to collect the remaining parts from Brian. He had them all waiting for us – new front bodywork, radiator ducts, headlight mouldings, from bodywork mounting frame. He also saved the day with a spare disk. Yay! :)

By the time we fought our way back through the Friday afternoon traffic it was 4.30. While Andy reassembled the nearside rear upright with the new disk I got on with fitting the front suspension mounts. Then he moved onto the front suspension and I fitted the new chain – because I’m going 3 teeth bigger on the rear sprocket the old one was too short and I didn’t fancy adding another couple of links to it. Once it was cut to length I riveted it on then got it adjusted. Once I’d refitted the pullrods the rear end was looking like this.

With both of us working on the front end we soon had the steering rods and pullrods fitted and it was looking a lot more like a race car again. Just needs the ARB rods fitting then the front end’s done. By now we were both pretty knackered and our families had been neglected enough so we called it a day and headed off for a couple of beers and a takeaway.

So, will I make Oulton Park next weekend? I still don’t know but I haven’t got to a point that tells me it’s impossible. I’ve got much of Saturday (working from 4pm) and all day Sunday to crack on with it although next week is a bit of a disaster! The finals are out and RGB is the next to last scrutineering session at 10.10 so driving up there on the Saturday morning is doable.